| Dateline: February 16, 2002
Shady Bend Airport; Real World Solutions Corporate Headquarters.
Paul Lamar, Editor of the Aircraft Rotary Engine Newsletter, showed up
yesterday with homemade water manometer in hand and
proceeded to shroud the RVotter in mass quantities of duct tape and
plastic tubing. The tubing was scientifically tipped with the finest
quality used sponge from Laura's kitchen.
Extensive flight testing yielded much interesting data. Of course, if
we tell you we'll have to kill you. Feel brave? Read on.
One of the most significant findings was that the right side radiator
had very little pressure differential from front to back . We also found that the
pressure in the cowl was higher then expected which suggested that cooling
could be improved at low speeds and climb with the use of a cowl flap.
We sealed the hole around the PSRU behind the prop spinner and actually
increased the pressure in the cowl slightly indicating that the spinner
is, in effect, pumping a small amount of air out of the cowl. However, we
could not detect a big difference in cooling during this portion of the
test. Tracy felt the drag was a little lower, but we have not completed
sufficient tests to confirm that suspicion.
The tests validated that the left side radiator and duct were working
well and full dynamic pressure was recovered in front of the heat
exchanger. This was 300% higher then the pressure recovery in front of the
right side radiator.
More rocket science will be conducted later using this highly
sophisticated and expensive equipment. |
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Pressure tap (and sponge) in front of right radiator. |
The RWS R & D Facility with
certified hot gluer attaching sponge to end of tubes. |
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Pressure lines taped to side of fuselage
from auxiliary pitot tube. |
In flight photo of water manometer with secret
formula fluid. |
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Flight test tech contemplating test results. |
Entire engineering staff of RWS saying
"I'm confused. How did this ever cool in the first place?" |
Test Data Analysis and corrective measures: July 18, 2002
Water manometers work by measuring how high a
column of water is pushed up
by air pressure. There are two columns for each manometer (with a
loop at
the bottom, like 'U') to keep the water from running out of the tube.
The
pressure between the two ends of the tube is the total distance between
the
water level in the 'U" tube. The sponge at the end of the
tube is to
ensure an average pressure at the location. If the air was
blowing into
the end of the tube without a sponge it would read the dynamic pressure
instead of the local average pressure. The 'magic fluid' in
the tubes was
water and food coloring.
How the data is viewed depends greatly depend on which phase of
flight
you want to optimize. Paul immediately zeroed in on the pressure
under the cowl and saw the need for a cowl flap. The most significant finding to me was the extremely low differential
pressure (1.75" H2O) across the right side radiator. The left
side rad had 300% more pressure than the right rad.
The pressure under the cowl was about 2.9" H2O. Paul thought
this was much
too high (he wants to see zero) and the most significant finding.
The local
pressure under the plane where the cooling outlet is was 1.1" H2O.
To give
some perspective, the total available dynamic pressure at the test
airspeed
(120 mph) was 7.61" H2O. The pressure at the left side cooling
inlet was
8.11 due to propeller slipstream.
Paul's perspective was that of the aerodynamicist, he wants a no compromise
cooling system that will operate at best efficiency in all phases of flight,
from maximum power climb at Vx to top speed in level flight with minimum
drag. About the only way to accomplish this is to have a cowl flap.
This can be anything from a hinged slat on the bottom edge of the cowl to a
sophisticated variable nozzle. The cowl flap is the only way to
significantly reduce the under cowl pressure without incurring a high drag
penalty at cruise speed. Lowering the cowl pressure would improve the
performance of all three heat exchangers (both radiators and the oil cooler).
On
the other hand, I'm thinking about what the easiest and quickest thing I can do
to improve cooling without taking the RVotter out of service for a long
time. Even a simple flap requires significant fabrication and some means
of actuating it from the cockpit. And cockpit space is at a very high
premium on an airplane like the -4.
My
priorities had me zeroing in on the poor pressure recovery on the front of the
right side radiator. Correcting this could be as simple as reshaping or
slightly enlarging the cooling inlet.
So,
what's the down side of going the simple way out? My fixed cooling outlet
was more or less optimized for minimum drag at cruise flight conditions.
This meant that it limits cooling at low speeds such as in a climb.
On a hot 95 degree day I have to limit full throttle climb to about 1
minute. This sounds like a severe limitation unless you look at the full
picture. At full throttle rate of climb, this means I am more than 2000
feet agl before coolant temps reach my conservative red line of 205 deg.
F. At this point I reduce power to keep the temps from going higher but
I'm still climbing at around 1000 fpm. This is better performance
than most factory built aircraft can give at full throttle. At this rate
of climb the plane is soon in the cool air at cruise altitude and the coolant
temperatures are coming down fast. Bottom line is that while the airplane
is not performing at it's best in all phases of flight, it doesn't have
much effect on flying the mission.
Having
rationalized my way out of fabricating a cowl flap system, I began hacking away
at the right side hole in the fiberglass cowl. I like to document changes
with before and after pictures but I got carried away and butchered the cowl
before taking any pix.
July 14 2002 turned out to be a perfect
day for cooling tests. The temperature was around 94 degrees with matching
humidity. I could see that the cooling was improved even before takeoff
because the engine took longer than usual to come up to minimum temp for
takeoff. My cooling system has no thermostat so the radiators start
cooling right away.
When
the oil temperature reached 135 degrees I firewalled the throttle and was
airborne in a matter of seconds and climbing at 2050 fpm. At 3000 feet the
coolant temperature was only at 200 deg F and I was ecstatic with the
improvement. The air was already cooling off a bit at this altitude
so I reduced power to cruise and descended down into the hot sticky air at 1000
feet. When the temperatures stabilized, I measured an 8 to 10 degree
reduction in coolant temp (compared to temp prior to cooling inlet change) and a
2 degree reduction in oil temp.
The
next question in my mind was how much drag the change had added. I'm sure
that there is some added drag but it was not measurable. Both cruise speed
at 7 GPH and top speed at full throttle was unchanged as close as I could
tell.
It is very rare
to be able to get this much improvement from such a small change. The key
to its success was identifying the deficiency in the system. It was Paul's
emphasis on the importance of pressure tests that accurately pointed to where
the improvements could be made so he deserves full credit for dragging me
kicking and screaming into doing them.
I'll
probably have to add Paul's beloved cowl flap too. But that can wait till
this winter when the cooling improvements will result in engine temperatures
never getting up to normal operating levels! A cowl flap will fix that
problem too.